X'Air V2(2), G-CBTY, 27 June 2004

X鈥橝ir V2(2), G-CBTY

Summary:

During climb-out following a touch-and-go the engine stopped abruptly and a forced landing was carried out. Both occupants exited the aircraft without difficulty. 皇冠体育app engine, a Simonini Victor 2 two stroke, twin cylinder, twin ignition, water-cooled engine, was examined and two burn holes were observed in the side wall of the rear cylinder head. 皇冠体育app plating on the top end of the inner walls of both cylinders was cracked and partially detached in places. Metallurgical examination of the engine bearings revealed long term corrosion within the roller bearing which had occurred whilst the engine was stationary. It was considered that the engine failure was caused by the loss of coolant to the engine allowing hot gases to burn through the cylinder casing. 皇冠体育app accumulation of liquid in the crankcase had probably resulted from a leak past one or both of the cylinder head elastomeric seals. 皇冠体育app engine had completed a total of 6 hours 45 minutes since 2003 at the time of the engine failure.

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Published 10 December 2014